Expert HVAC Service and More in West Bradford Township, PA
DiBiase Heating and Cooling Company provides a full range of services to keep your home comfortable and efficient year-round in West Bradford Township, PA. Whether you need HVAC repair, installation, or maintenance, we’ve got you covered. Our team also specializes in improving indoor air quality with air purifiers, humidifiers, and ductwork services. Looking for water heater solutions? We offer repairs and replacements for both tank and tankless systems. Additionally, our energy services, including air sealing, insulation, and energy audits, help homeowners save on utility costs while maximizing comfort. Whatever your home’s needs, DiBiase Heating and Cooling Company is here to deliver expert service.
Founded in 2008, DiBiase Heating and Cooling Company is a family-owned and operated company that’s committed to delivering honest, reliable service. We take pride in our expertise, offering certified technicians who provide top-quality HVAC, plumbing, and energy services. What sets us apart is our focus on process and integrity—we do the job right the first time, ensuring your home is always in good hands. Ready to experience the DiBiase difference? Call 610-873-1244 or contact us online today to schedule your service!
Recent Jobs and Reviews in West Bradford Township, PA
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- Valley Township, PA (4)
- Wayne, PA (9)
- West Bradford Township, PA (21)
- West Brandywine Township, PA (3)
- West Chester, PA (72)
- West Grove, PA (2)
Job Locations and Reviews
no heat call customer was down by the furnace and a smell like a burning smell found system off upon. Set thermostat to heat and checked operation. Error code was registering on the board pressure switch code. No operation from inducer assembly check voltage to motor. 115 removed ineucer to inspect wheel, wheel is very hard to spin. New inducer is needed. Called manufacturer and order new motor. Customer paid in full for repairs. We will be coming back tomorrow between 8 and 12.
The noise issue was a couple of registers in living room and Dino room. High velocity, The air handler was ramping up to a high blower speed because the aux heat was configured without a lockout set point. And droop was set to 00. So the equipment would run up with aux heat and therefore ramp up blower speed. I set aux heat lockout to 45°F. The unit will only run at high blower speed if it drops below 45°F now. I also checked outdoor unit wiring and for any abnormal sounds. Ok Explain p d that there is a 5 minute compressor lockout period to protect compressor. So once outdoor unit shuts off there is a 5 min period before it will energize again. System operating well at this time.
Completed heat tune up for 80,000 BTU Goodman furnace/ 2 zones EWC zone panel. Zone dampers are above drywall ceiling. 16x25x1 filter in good condition Inspected burners, heat exchanger, inducer assembly, pressure switches, Cleaned flame sensor and verified operation Ignitor in good condition, measured ohm value Confirmed manifold gas pressure Inspected wiring, controls, electric motors. There is no surge protection. Left email estimate. Inspected drain. There is a wet switch but AC drain has no ez trap or overfill protection switch so I left estimate for EZ trap. Measured temperature rise and static pressure. Combustion and smoke tests pass Furnace operating well at this time.
Completed heat tune up 80,000 BTU Goodman furnace 16x25x1 Filter in good condition. It is MERV 13, temperature rise a little high. I recommend using MERV 11 or lower. If you use MERV 13, replace every 2 months. Inspected burners, heat exchanger, inducer assembly, pressure switches Cleaned flame sensor and verified flame rectification circuit Ignitor in good condition, verified ohm reading Confirmed proper manifold gas pressure Inspected wiring and controls. No surge protector, left email estimate. Checked drains. There are no water safeties left estimates for EZ trap and wet switch. Combustion, smoke and draft tests: Pass System operating well at this time.
Completed (2) heat tune ups for hybrid systems. 2nd floor furnace located in garage above ceiling 40,000 BTU propane 1st Floor located in basement 80,000 BTU propane Filter for second floor was clean, left additional Replaced filter for 1st floor system. For EACH furnace: Inspected heat exchanger, burners, inducer assembly, pressure switches Cleaned flame sensor and verified flame rectification circuit Checked ignitor, measured ohm reading Confirmed manifold propane pressures Measured temperature rise and static pressure Tested defrost operations. Inspected wiring, controls, electric motors and components: left estimate for ECM surge protector for st floor system. The other system has surge protection at indoor equipment Combustion and draft tests: Pass Aprilaire 35 water panel for basement humidifier in good condition. Verified operation. The 1st floor system condenser fan grille was misaligned and the blade was hitting the shroud. Fixed this today but moving grille sl
Upon arrival for oil maintenance I changed the filter, nozzle, and strainer. Filter was in bad condition for a year. Tank is underground so this is indicating issues with tank. Tested transformer. Replaced electrode kit. Unit was terribly sooted up. I cleaned heat exchanger, flue, and chimney. Turned on hot water and all three zones. Bled the air out of the oil line. Checked operation of the circulator pump and amps. Checked operation and response of aquastat. Tested all three zones and zone valves. Performed and combustion test and it was terrible. 3% 02 and 700 CO ppm. Adjusted airband and cleaned hair and dryer lint from it. Achieved a much better reading after making adjustments. Performed a smoke test as it was a 1. Unit is in normal operation at this time.
Technician added check payment twice on invoice #43050. Invoice created to zero out credit on profile.
Gas furnace tuneup on a 90% Checked the air filter and found good. #35 panels were replaced supplied by the customer . Checked the wiring connections and the voltages . Inspected and tested the burners and flame sensor and igniter. Flushed and tested the drain lines and furnace trap . checked the thermostat in heating mode and checked the gas pressures and the furnace safeties. Inspected the flue pipe and fresh air for bellies. checked the motor amps on the inducer operation and blower motor . Took indoor heat temp rise and tested for combustion. everything is in good working order at this time of service.
On arrival found indoor unit for second floor was Calling for cooling. But the outdoor was not coming on. Customer had said she smelled something burning over the weekend was going to call to address. The burning smell had nothing to do with the new system. New system just had the outdoor breaker trip tightened up the breaker connections, No charge. Did find on second floor system, had a failed Start assist kit quoted for new kit and collected for diagnostic. Both systems are back up and running at this time service .
Upon arrival for maintenance on gas furnace I changed air filter. I noticed the rust inside the unit and saw that it was coming from inducer boot so i tightened clamps up and water appeared to stop. I cleaned the flame sensor. I inspected heat exchanger and burners. I checked blower motor and assembly. I checked the resistance of igniter. Checked all wiring and control board. I checked inducer operation and ensured hose port was clear. I checked gas pressures. Checked air temperature rise. Performed combustion test. Unit is in normal operation at this time.